I converted my S7 to poly-vee belt primary and secondary drives back in 2012, since when I've had a problem that is sort of resolved, but not entirely.
To cut the grooves in the countershaft and spindle pulleys the otherwise finished pulleys were mounted on mandrels, and the grooves cut with a professionally ground HSS form tool, to ensure correct form and concentricity. The grooves run true to better than 0.0015" radial and axial run-out.
When running on the 2105rpm speed setting (and only on the 2105 range) , the headstock develops a clattering noise, positively identified as being caused by the spindle pulley moving laterally on the spindle and bumping into the back gear.
If I assemble the headstock without the back gear in place (so that the pulley has no restriction to its lateral movement) and run just the pulley, it shuffles around by something like 0.020", perhaps a bit more.
The shuffling gets worse as belt tension is increased, only disappears when the tension is so low as to be all but useless.
Now for the strange bit – it does this once per BELT revolution, which seems to suggest that the pulleys are ok, and indeed they seem to be – see above.
I've tried 3 different belts – Pixar (came with the Hemingway kit), Optibelt and GoodYear. All do the same thing.
I tried biasing the pulley shuffle towards the tail end of the spindle (to stop it hitting the bull wheel) by shifting the countershaft pulley leftwards, to try to hold the spindle pulley against the angular contact bearing assembly. But to stop the rattling the pulley has to be so far offset as to cause the belt to protest.
I discussed the shuffling problem with someone who is expert in poly-vee belts, he had not come across this before. He suggested it might be worth cutting a belt down to 4 ribs, as 6 ribs (as designed) was possibly over-belting the machine.
I did that, it might have made a small difference to the shuffling motion, but nothing significant. However, it did make a difference when trying to bias the movement – the countershaft pully only needed to be shifted left by less than half a groove width to stop the spindle pulley hitting the bullwheel, and the belt seems happy enough with that.
So that's how the machine's running now, no rattling and working ok. But I don't like things that I can't understand, and the solution is a bit of a bodge. I'd rather have it right, full stop!
So, can anyone shed some light onto this strange phenomena?