Been a busy week making things foolproof on the flash steamer after last Sundays first 2015 speed trials at Kingsbury Water Park.
The first run recorded 121mph I thought what have I done wrong is it the larger exhaust exit on the new generator case or the repaired Tig welded generator it's my first attempt at reclaiming a burst generator.
Fortunately a 3mm allen screw that adjusts the water and fuel pump strokes had worked loose it's normally locktighted but as it's awkward to adjust thought it would be ok not to bother this time.
Second run was spectacular unfortunately I timed too early as it was taking a long time to build up speed lap after lap was going faster and faster so started the timing.
124mph was recorded but if timed a few laps later would have been 130mph.
The weather was turning cold and rough for the final run and only a few dedicated souls remained under guidance from John-De Mott we waited for the speed to build up and recorded 127.8mph.
When stripping the engine at home found the curved cam follower-retaining pin was missing a part that is diligently checked for tightness the first time over many years this has happened.
So apart from simple fixes have been making a batch of new hairpin valve springs the key to maintaining the high rpm on the two stroke steamer then a friend with a request to make a stainless flower holder for his Fathers grave plus getting the 1990 Renault ready for the MOT it has been a busy week.
A keen photograther friend Roger Walton wanted to take some pictures before I stripped it so here is one.
