4″ independent lathe chuck recommendations and holding capacity

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4″ independent lathe chuck recommendations and holding capacity

Home Forums Beginners questions 4″ independent lathe chuck recommendations and holding capacity

Viewing 6 posts - 26 through 31 (of 31 total)
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  • #245947
    Michael Gilligan
    Participant
      @michaelgilligan61133
      Posted by Michael Gilligan on 08/07/2016 21:11:10:

      Perhaps I should re-weigh mine on some better scales.

      .

      With apologies for any confusion that I may have caused …

      I have re-weighed my 'threaded body' Pratt-Burnerd 6" on some good [but uncalibrated] Kitchen Scales, and the indicated weight is 4358g … Which seems consistent with Nick's weighing.

      It appears that my Bathroom Scales are reading low [… now there's a surprise! ]

      MichaelG.

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      #245956
      Neil Wyatt
      Moderator
        @neilwyatt
        Posted by Michael Gilligan on 09/07/2016 14:10:49:

        Posted by Michael Gilligan on 08/07/2016 21:11:10:

        Perhaps I should re-weigh mine on some better scales.

        .

        With apologies for any confusion that I may have caused …

        I have re-weighed my 'threaded body' Pratt-Burnerd 6" on some good [but uncalibrated] Kitchen Scales, and the indicated weight is 4358g … Which seems consistent with Nick's weighing.

        It appears that my Bathroom Scales are reading low [… now there's a surprise! ]

        MichaelG.

        Use the scales on carpet.

        **LINK**

        Neil

        #246034
        bodge
        Participant
          @bodge

          Hi Micheal

          Yes thats pretty much how i would go about it , the only bit i have a bit of a problem with, is how does one ensure a good fit of the mandrel screw thread in the new bush. When i did similar mod, fitting a 4 inch lever scroll chuck to a 3/4 inch mandrel, the chuck was internel threaded 24 x 1.5 mm, the mandrels threaded 3/4 x 10w. But i had another lathe to make the bush with, i removed the 3/4 mandrel from the lathe so i was able to use the mandrel to test the internal thread when i was getting close to finished size, cutting with single point tool using lead screw, so was able to use the mandrel to gauge and get best possible fit,

          Next the 24×1.5mm male thread was cut again using single point tool again thread was tested using the chuck to gauge the thread to get best fit, next face off the bush just enough get clean square end, the bush was then counter bored, as the 3/4 mandrel has straight 3/4 register about a 1 or 1 1/2 tpi, so the mandrel can now be screwed fully home,,( it is of course now the wrong way round ) remove mandrel

          Part off… Then set mandrel up on the lathe with fixed steady using pair of clock gauges to set running true, then screw bush onto mandrel counter bore for register and face off the parted off surface, about 1/2 a thou concave, remove bush from mandrel turn through 180` refit to test ( the bush is now the right way round ) and very light facing cut with tool to make shoulder side of bush very slightly concave, these last two opps ensure the mating surfaces are full contact across the diameters

          Fit chuck check and test , all`s well , reunite mandrel with lathe.

          Just a slight variation Micheal, and think your list of opps is fine , will the bell mouthed chuck hold true! If really bad one could use a longer blank and use a fixed steady, this would remove the wobble factor of the bell mouthed jaws so all the chuck has to do is revolve the work piece

          There was bit more to the above in as much as the blank i used was long enough to make two adapters, the other one to be threaded male 11/8 myford so that was faced off and bored and screw cut 3/4w and counter bored for register before removing from chuck, the myford thread can now be finished at later date on the 3/4 mandrel lathe.

          Simple`s…………..b

          PS If you blow my one and only pic up you can see the bush fitted to the chuck, the chuck is jaws down on the boring table , right hand side near the top , sorry its such poor res…. if i proof read this any more it wont get posted hope it makes sense…………..b

          edited for typo error and may still have missed others !   oops……………b

          Edited By bodge on 10/07/2016 00:17:48

          I should of added that the myford threaded adapter is so as i can use 80mm 3 jaw i have that has 11/8 myford back plate and 4inch 4 jaw ind, if and when i get round to buying one, 

          Edited By bodge on 10/07/2016 00:32:46

          #246038
          bodge
          Participant
            @bodge

            Hi typo on my last post, fourth line second para . should read counter bored to a depth of 1 or 1 and 1/2 teeth of thread, just had a look and yes its not much about one and half teeth.

            It was easier to make than to write about it……………b

            Edited By bodge on 10/07/2016 01:24:58

            #246060
            Michael Gilligan
            Participant
              @michaelgilligan61133

              Thanks for the 'sanity check' on my list of ops, bodge yes

              … It really doesn't seem difficult, and the only tricky work is being done on 'a bit of bar' [repeat until satisfied]

              As you say; if the old bell-mouthed chuck is really bad; a fixed steady might be needed … but that could be a disposable item, knocked-up from a few bits of wood.

              MichaelG.

              #246080
              bodge
              Participant
                @bodge

                Hi MichealG

                Your welcome for the "sanity check" I had to proof read it a fair few times myself to make sure i wasnt losing the plot. The major difference is i needed 24 x 1.5 mm instead of plain o/d on the bush plus the shoulder made for a few more ops, yes disposable fixed steady would be ok for a one off.

                I didnt think it was difficult while i was making the adapter the job flowed along quite smoothly, plus i also got second adapter half made in the first set of ops, and the end result was on the money ie the chuck ran true when the mandrel was re installed in the head stock and the chuck clocked true when fitted on the mandrel………to be honest it was harder to write it up than make it………………bodge

                When screw cutting i like to use Ghts method offset top slide but its set so the tool also takes a light cut on trailing edge of the tool while the leading edge does most of the work, it works well for me……b

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