Myford ML4 Restoration: Headstock bearings and spindle removal

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Myford ML4 Restoration: Headstock bearings and spindle removal

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  • #467722
    Luke Mitchell
    Participant
      @lukemitchell30627

      Hello all.

      Firstly, I am a first time poster here. I found the site after looking for other ML4 restorations (of which there seems to be precious little, at least not publicised on the internet).

      I have recently inherited the lathe from my grandfather. It was his brothers and he doesn't have a great deal of information about it – save that it was often used and clearly loved. It has sat now for a long time, a decade or more, and is in need of some love.

      I stripped down, cleaned and lubricated as much of the lathe as possible and I've managed to turn a few simple projects using it: a sink plug, made using brass; an arbor for an angle grinder; boring out a pulley wheel.

      On aluminium and brass I can get a fairly good finish. When parting, or cutting steels, however there is a lot of vibration and chatter and a whirring sound from the headstock. There is also a little vertical play in the spindle (about 0.2mm, measured using my cheap DTI) and a little run-out (0.03mm).

      I was told that the headstock bearings would need replacing and my experience turning seems to confirm this.

      This evening I carefully adjusted the clamp bolts in the headstock, taking care not to over-tighten them as I've read this can split the casting. I then nipped up the grub screws until the spindle seized, then backed off 1/4 turn. This operation eliminated much of the vertical play (it was reduced to ~0.05mm). However, when I powered up the lathe and began turning it produced an awful chatter even during shallow cuts. Slackening the clamp bolts helped but brought back the play.

      I believe the vertical play is making parting, in particular, very difficult. More than once the work has jumped onto the parting tool.

      Some details about the lathe:

      • 1.1/8" x 12 TPI thread on the spindle nose
      • 3.1/2" height between center and ways
      • MT2 in the spindle
      • MT1 in the tailstock
      • Tumbler reverse
      • "Newer" tailstock casting with large dovetail gib
      • Toolpost bolt has been re-tapped to M10 at some point

      The spindle thread leads me to suspect it is a later ML4 as this is the same (I believe) as the ML7. The serial number has been painted over however and so I cannot use this to age the machine.

      Some (slightly random) photos:

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      #13860
      Luke Mitchell
      Participant
        @lukemitchell30627
        #467724
        Luke Mitchell
        Participant
          @lukemitchell30627

          (Post continued…)

          At some point I would like to completely strip, sandblast and repaint the castings. I may also have the ways reground as they are a bit worse for wear. For now, however, I would like to get the machine up and running and usable.

          Also on my to-do list is to replace the motor and the belts. The original motor sparks when powered on and is in need of a good clean and possibly a re-wind. I have a new 3ph motor with a VFD waiting to be installed but the cabling appears to be lost in transit (the post is a little crazy at the minute). When the new set-up has been installed I'll order two new belts and tension them correctly.

          I am now intending to remove the spindle to examine it and, if necessary replace the bearings. I'm a little scared about this operation as, at the moment, I can't see any obvious way to remove the spindle.

          The attached gear on the left-hand side seems to be stuck – it looks to me as though there should be a locating pin or bolt but, if so, this is missing and there is just an offset hole (see last photo).

          Has anyone removed an ML4 spindle and, if so, could you please describe how to do so?

          I hope this was of interest to some of you and, if anyone who is a former/current owner of one of these lathes has any advice, I'd gratefully receive it.

          Kind regards and stay well

          Luke

          #467790
          Brian Wood
          Participant
            @brianwood45127

            Hello Luke,

            Welcome to the Forum, I hope collectively we can help you.

            I inherited my late father's ML4 which he bought new in 1945 and did a lot of work with it, including much of the machining for my Dore Westbury milling machine, Later I had the opportunity to replace it with a good ML7 which I bought from an old friend I trusted. I therefore grew up with Dad's lathe from about 7 years old. I was sad to see it go, it was still a good working lathe.

            The gear on the spindle driving the change wheel gearing is a very tight fit on the spindle and locked by [ I think] a 2 BA screw across the joint to prevent creep. It will pull off or can be carefully levered off. Behind that is a screwed collar to adjust spindle end float; that is secured with a grub screw onto the fine thread. It should have a copper disc preventing thread bruising so look out for it when you dismantle. If absent a suitable size of brass washer will do as a substitute. Thinking back now, I seen to remember using the screwed collar as a jacking tool to push the gear off the spindle..

            The pulley cluster is secured to the spindle with a grub screw through the collar into a dimple in the spindle. It should spin freely on the spindle as part of the back gear operation when slow spindle speed is called for.

            The 65 tooth bull gear has yet another grub screw to grip the spindle. If I remember correctly, that frequently needs tightening if doing a job with interrupted cutting, the jarring slackens it's grip. These bull wheels are very prone to losing teeth if the back gear cluster is engaged a touch too early. I have a spare if you need it.

            With the end gear and thrust collar removed, the spindle can be withdrawn towards the tailstock, having slackened the bearings of course. There are no Woodruff keys to catch or interfere with that, although you may have to wriggle the shaft out. In removing it you will reveal the thrust bearing at the chuck end that is buried inside the bearing housing

            I noted the care you took over bearing adjustment to avoid overtightening. When you come to re-assembly it might pay you to make up two inserts for the gap, lapped to fit each, so that you can close the bearing down onto something and make a 'solid' bearing of it. Drill a hole through these so that they are held captive by the bolt.

            I don't think you will be able to buy new bearings for this model any more. The grub screws you referred to with regard to these bearing were I think locking features preventing rotation within the bearing housing. They certainly play no part in adjustment.

            The degree of bearing wear in the white metals and on the spindle itself are really matters of judgement and to be set for minimum shake consistent with free running; likewise the degree of spindle end float. The bearings should get warm in operation but not above that in say 1 hour's running. They must not get hot. Lubrication is of course important and I found a standard SAE 30 grade oil perfectly satisfactory

            I too had trouble with parting off and in the end decided to adopt the coward's way out with a hacksaw, taking precautions below the cutting with a block of timber to prevent damage to the lathe bed. I suspect much of the snatching and vibration arose from any slack in the gib adjustment across the bed for the rather narrow cross slide which would give rise to 'nodding' and other such trouble. One of your pictures shows a paring tool used upside down, that is another dodge with the lathe running in reverse, but getting the tool height on centre that way round can be a problem.

            Dad's lathe had the original design of tailstock bed clamp and what a dreadful thing that was to set up. In the 1960's Myford did offer to rebuild owner's tailstocks with a new bed shoe and proper cross piece so that offsets could be made, but it was of course an expensive job and I never had the cash to cover it. Your version is one I have not seen before and looks a good deal better than the one I struggled with.

            I think that is enough for the time being; I hope it has been of use to you.

            Kind regards Brian

            #467795
            Luke Mitchell
            Participant
              @lukemitchell30627

              Hi Brian, and many thanks for taking the time to give me such a detailed reply.

              I'm a little concerned that the spindle gear has seized onto the spindle. You mention that it is a very tight fit – it certainly seems so! It also appears that the 2BA screw has been lost on my machine and that the gear has slipped a little over time. I've included a photograph below.

              I will have a think about the best way to remove the gear. I suspect I will have to lever it out against the collar, as you mention that you once did. If possible, it would be nice to fasten something securely around the teeth (somewhat like a collet) and to pull it off that way as I suspect it will reduce the chances of causing any damage. If anyone has any bright ideas please let me know!

              Another question I have is concerning tee-bolts. I have measured the slots as best I can and they appear to be 3/8" at the narrowest width, 3/8" deep and a shade over 1/2" wide at the bottom (I measure 13.5mm which is actually 17/32" ). Does this sound usual?

              Also, short of making my own (I have no access to a mill, unfortunately), does anyone know a good source for some tee-bolts so that I can use an angle plate and make up a rear tool post.

              Kind regards.

              Edited By Luke Mitchell on 29/04/2020 10:49:45

              Edited By Luke Mitchell on 29/04/2020 10:49:57

              #467811
              Brian Wood
              Participant
                @brianwood45127

                Hello again Luke,

                You are quite correct, that gear has slipped and in the direction you would expect it to go for spindle creep with respect to the gearing for a prolonged cut.

                Your fear it has seized is I think somewhat premature. It WILL lever off with two slim blades opposed to each other. A bit of heat on the gear before you start will help it a lot. When I said I had used the screwed collar as a jack, I meant just that. Lock the spindle and make use of the fine thread the collar is fitted with to push the gear off, or at least open the gap between it and the gear to allow flat bladed screwdrivers into the joint to 'walk' the gear off. Don't be tempted to ease the fit to help it back on later, it needs that degree of interference fit..

                Myford sell Tee headed bolts in a range of lengths. They used to sell a rear tool post as well but it wasn't a cheap accessory.

                Kind regards Brian.

                #467821
                Luke Mitchell
                Participant
                  @lukemitchell30627

                  Hi Brian, and thanks for your continued advice.

                  I'd not realised that the screwed collar was threaded – I've loosened the grub screw and found that it will rotate a small amount but, not having been able to fully extract the spindle, I didn't realise it was fixed using thread – I'd assumed, naievely, that the collar was unable to rotate as it was a little deformed.

                  I will have a go at the removal over the next week or so and report back with some photographs.

                  Many thanks

                  #467950
                  Luke Mitchell
                  Participant
                    @lukemitchell30627

                    Hi Brian (or others),

                    I wonder if you could clarify something for me: what is the best/safest way to lock the spindle? I don't want to engage the back gear as it's already missing two or three teeth and I've read, on other posts, that this is a common mistake. I could nip up those grub screws that I mentioned as this seems to pin the spindle in place but I don't think it would hold it very securely…

                    Kind regards,

                    Luke

                    #468027
                    Brian Wood
                    Participant
                      @brianwood45127

                      Hello Luke,

                      One way is to clamp the drive belt on the spindle, when tensioned, and let the clamp rest against something solid. A second approach is to bridge the chuck jaws with a section of wood having the free end resting against the lathe bed. You might unscrew the chuck with this method

                      The usual approach with the backgear locked leads to the risk of tooth damage as you have pointed out. I would not advise any approach with the bearing grub screws, for a start I don't really know what function they serve and secondly the bearings may get damaged in the process.

                      I said earlier and will repeat it now, heat the gear, apply WD 40 in the joint between the gear and spindle and use slim levering tools as an opposed pair in the gap between the end play adjusting collar and the gear itself to push the gear off. There will then be no need to lock the spindle.

                      I do have a spare bull wheel which you may care to build in when you reassemble the spindle. Send me a PM if you are interested

                      Kind regards Brian

                      #468240
                      Luke Mitchell
                      Participant
                        @lukemitchell30627

                        Right, I got the spindle off thanks to Brian's instructions.

                        I first used the collar as a jack, as suggested, and managed to create a gap of 1mm or so. It was very stiff and I used a load of WD40 and a blast with the torch to help.The gear was then walked out, very carefully, using various screwdriver tips and the collar as a levering point, taking gear not to gall the spindle or deform the gear. It took about 30 minutes and three (gentle) heats with the propane torch (this makes a big difference).

                        I "locked" the spindle by gripping a piece of 1/2" brass hex stock in the jaws and holding this using a long ring-tipped wrench.This is the same method I have used to free a stuck chuck, clamping the pulley wheels or bull wheel using a strap clamp.

                        The missing bolt was indeed 2BA and would have been rather short. I have a few spares and I've been replacing them as I find them – the ones on the lathe were pretty perished and the slots very enlarged. I'll have to cut one down to fit when I reinstall everything. I may have to clean the thread up a bit, as you'll see in the photos.

                        The gear looked a bit beaten up. There is a chance that I contributed a little, given my choice of wedge to remove it, but I suspect it was already rather damaged. The teeth were certainly damaged on the collar side before I began and it looked rather "squashed" against it. I'll clean it up with a stone.

                        I then removed the 0BA (x 3/8&quot grub screw in the collar and unscrewed the collar from the fine thread.

                        I removed the 0BA (x 3/8&quot grub screws from the pulley assembly and the bull wheel. The grub screw in the bull wheel was loose and it was able to partially rotate. When I removed the spindle I could clearly see that this had caused some damage.

                        Finally, I loosened the adjustment bolts in the split castings.

                        The spindle was a bit stiff going through the left-hand bearing and needed gently tapping through with a rubber mallet. When the tip of the spindle could not be tapped directly I used a small piece of hardwood. I didn't need to apply much force at all to do this.

                        #468241
                        Luke Mitchell
                        Participant
                          @lukemitchell30627

                          Here are some photographs of the casting, spindle removed. The left-hand bearing can be seen in place. It had clearly spun at some point and the oil hole was some 90 degrees off. The right-hand bearing came out with the spindle and I took the opportunity to take a look at the casting (which has quite a few voids).

                          I hope those images are interesting to someone. Whilst I'm posting them it occurs to me that there are rather a lot of them!

                          #468242
                          Luke Mitchell
                          Participant
                            @lukemitchell30627

                            Here is a look at the spindle. Honestly, I have no idea how bad the wear is but it doesn't look great to my eyes. There are quite a few mars and some obvious damage, on the left-hand side as photographed. I believe this is from the grub screw of the pulley assembly but I'm not certain. The pit caused by the bull wheel is visible just to the left of the bearing, on the right. There are also obvious grooves where the edges of the bearings sit.

                            More positively, the shoulder that butts against the right-hand bearing casting seems to be in very good condition. I guess there hasn't been much wear there due to the thrust bearing. The original machining marks (I think) can still be seen.

                            The thrust bearing itself seems in quite good shape too, although I profess that I'm not sure how to tell. I removed the old grease and it spins fairly freely, although there is a little noise as I tested it. I can't see any marks in any of the ball bearings. I'll put some grease on it and try again.

                            #468244
                            Luke Mitchell
                            Participant
                              @lukemitchell30627

                              I could feel a little play in the bearing which remained on the spindle as I extracted it and I tried to photograph this to illustrate it. It appears that the gap is something around 0.5mm. I should have used a feeler gauge but I didn't have one to hand – I can try that later. The gap can be seen in the following photograph (the bearing is pushed flush with the spindle on the underside).

                              I removed the bearings from the spindle, cleaned off the old, grimy oil and put everything in bags for tomorrow. I could see a few high spots, blunt burrs that I can carefully stone down, but mostly the damage was indentation.

                              Here is the second bearing. This one looks to be in a slightly worse state that the one that remained in the casting. I believe that the damage to the spindle held it in place as it was removed. The same damage rubbed on the bearing as I removed it from the spindle – you can see a spiral where I twisted the bearing free. This is even with a liberal heat using the torch beforehand.

                              Please let me know what you think/suggest. Is the damage excessive for a usable machine or is this "normal" wear and tear for a machine of this age?

                              Kind regards

                              Edited By Luke Mitchell on 30/04/2020 23:45:00

                              Edited By Luke Mitchell on 30/04/2020 23:45:17

                              Edited By Luke Mitchell on 30/04/2020 23:46:24

                              #468262
                              Luke Mitchell
                              Participant
                                @lukemitchell30627

                                Morning all.

                                It has just occurred to me that, given the split nature of the bearings, any play may well be removed by tightening down the adjustment bolt when it's reinstalled. I'd still appreciate any thoughts or suggestions that anyone may have.

                                #468270
                                Luke Mitchell
                                Participant
                                  @lukemitchell30627

                                  I’m afraid I can’t see any way to edit the above posts but it seems that hosting via Google hasn’t worked as well as I hoped.

                                  Here is a link to the photos uploaded somewhere else.

                                  Edited By Luke Mitchell on 01/05/2020 07:53:23

                                  #468281
                                  SillyOldDuffer
                                  Moderator
                                    @sillyoldduffer
                                    Posted by Luke Mitchell on 01/05/2020 07:51:59:

                                    … it seems that hosting via Google hasn’t worked as well as I hoped.

                                    Here is a link to the photos uploaded somewhere else.

                                     

                                    Some of the Google hosted photos are working, others not. The failed images are asking for a google login. I guess the likely cause is a setting on your Google Account that declares photos to be Private (only the owner can view them) or Public (open to the world.) Each photo may have to be set 'Public' individually.

                                    Worth fixing if you can. Although Imgur displays the album, it loses the context of the photos to your original posts, making it painfully hard to decode what's going on. I think if you open the door to Google, the images in your earlier posts will automagically appear.

                                    This forum has a slightly clunky approach to hosting photos. You can either link to images hosted by someone else, or load them into an Album stored on this website. Links to remote images are more likely to break and not just because they want a login! The Album is safer, but more fuss. Easy enough when you get used to it. Neil describes how it's done here.

                                    Dave

                                    Edited By SillyOldDuffer on 01/05/2020 09:16:51

                                    #468283
                                    SillyOldDuffer
                                    Moderator
                                      @sillyoldduffer
                                      Posted by Luke Mitchell on 01/05/2020 07:12:16:

                                      Morning all.

                                      It has just occurred to me that, given the split nature of the bearings, any play may well be removed by tightening down the adjustment bolt when it's reinstalled. I'd still appreciate any thoughts or suggestions that anyone may have.

                                      Yes, but approach with extreme caution. Very likely this has been done a few times already. If the bearing is badly worn, it's possible to crack the headstock by screwing it down too far. Remember the bearings of a lathe this old might be worn out, don't push your luck! I'm no expert on these lathes, best wait for an expert to comment on what to do about bearings.

                                      Dave

                                      #468287
                                      Luke Mitchell
                                      Participant
                                        @lukemitchell30627

                                        Hi Dave, thanks for your advice regarding the images. Unfortunately I can't find a way to open up the sharing settings for those images, to my knowledge, they were already added to a "Shared Album". Perhaps I inadvertently copied the image link from my main album rather than the shared one. If a moderator is able to give me access to those posts then I will update them with new, working image links.

                                        Thanks also for your concern about cracking the headstock casting. Believe me it's at the forefront of my mind. I will only attempt this with caution as I'd rather have a complete, if wobbly lathe than a broken one.

                                        I'll gladly wait until another voice or two weighs in before doing anything though.

                                        Happy Friday

                                        #468310
                                        Brian Wood
                                        Participant
                                          @brianwood45127

                                          Hello Luke,

                                          This might become rather lengthy

                                          Part 1

                                          Do first of all remember this is now an old machine, pushing 80 years old or so, that was built and priced to serve a market worn down by the events of the time with the inevitable shortages of material the makers were able to squeeze from the diversions in support of the war effort at the time. That said, I think it is in remarkable condition really, given what has happened in the intervening years.

                                          I have never seen a bare ML4 headstock without bearing shells before, so I am learning things along with you. The following points may be helpful.

                                          • The spindle, as judged from your photos looks in good shape externally. The scarring and burrs can all be cleaned up with a fine cut broad file, used just enough to get the high spots and ridges down to the spindle surface.
                                          • The inside of the bearing shells again appear to be visually sound and probably good enough to be used without resorting to scraping. That is skilled work and needs the right shape of scraper to remove metal where needed. I would avoid doing any work of that nature if you have no such experience.

                                          You have not described the fit of the rear bearing shell in the housing. For it to have rotated, the grub screw holding it must have been slack enough for it to have ridden over the dimple made for the grub screw to secure it. Now that you have it out, is it a sloppy fit in the housing? If not, then well and good.

                                          Otherwise, salvage of the shell is possible by building up the outside with soft solder and dressing that to make a the shell snug fit in the housing.

                                          The thrust bearing is also quite likely to be in sound condition. Wash all the components thoroughly in petrol and dry it off. Inspect the flat washer faces for indentations, a generally polished looking wear mark is quite normal. Reassemble it loose on the spindle and gently spin it, dry, to listen for other that smooth bearing noise. It should not be lumpy and rough. New bearings to that pattern can be bought—-see suppliers at the end of this posting

                                          The casting itself looks fine, casting porosity is to be expected and yours is quite normal—nothing to worry about

                                          The 25 tooth gear. If you have a slim, fine cut file [like a magneto file for example] carefully file down the ragged edges that were adjacent to the thrust collar. I think the gear had been pushed on too far before which might explain the rather shallow depth of 2 BA thread locking it. Otherwise, the rest of the teeth look to be a usable condition

                                          Art 2 follows

                                          #468312
                                          Brian Wood
                                          Participant
                                            @brianwood45127

                                            Hello Luke,

                                            This might become rather lengthy

                                            Part 1

                                            Do first of all remember this is now an old machine, pushing 80 years old or so, that was built and priced to serve a market worn down by the events of the time with the inevitable shortages of material the makers were able to squeeze from the diversions in support of the war effort at the time. That said, I think it is in remarkable condition really, given what has happened in the intervening years.

                                            I have never seen a bare ML4 headstock without bearing shells before, so I am learning things along with you. The following points may be helpful.

                                            • The spindle, as judged from your photos looks in good shape externally. The scarring and burrs can all be cleaned up with a fine cut broad file, used just enough to get the high spots and ridges down to the spindle surface.
                                            • The inside of the bearing shells again appear to be visually sound and probably good enough to be used without resorting to scraping. That is skilled work and needs the right shape of scraper to remove metal where needed. I would avoid doing any work of that nature if you have no such experience.

                                            You have not described the fit of the rear bearing shell in the housing. For it to have rotated, the grub screw holding it must have been slack enough for it to have ridden over the dimple made for the grub screw to secure it. Now that you have it out, is it a sloppy fit in the housing? If not, then well and good.

                                            Otherwise, salvage of the shell is possible by building up the outside with soft solder and dressing that to make a the shell snug fit in the housing.

                                            The thrust bearing is also quite likely to be in sound condition. Wash all the components thoroughly in petrol and dry it off. Inspect the flat washer faces for indentations, a generally polished looking wear mark is quite normal. Reassemble it loose on the spindle and gently spin it, dry, to listen for other that smooth bearing noise. It should not be lumpy and rough. New bearings to that pattern can be bought—-see suppliers at the end of this posting

                                            The casting itself looks fine, casting porosity is to be expected and yours is quite normal—nothing to worry about

                                            The 25 tooth gear. If you have a slim, fine cut file [like a magneto file for example] carefully file down the ragged edges that were adjacent to the thrust collar. I think the gear had been pushed on too far before which might explain the rather shallow depth of 2 BA thread locking it. Otherwise, the rest of the teeth look to be a usable condition

                                            Art 2 follows

                                            #468323
                                            Luke Mitchell
                                            Participant
                                              @lukemitchell30627

                                              Hi Brian. Once again, thank you for your valuable input.

                                              It's good to read that the wear seems to be normal, or at least expected. It's also nice to see you write that the lathe seems to be in good condition; certainly it will have been well maintained by my relations during use – I know it has sat idle for at least one long period, however.

                                              I'd not considered the socioeconomic background to the manufacture of this lathe before but it makes complete sense that resources (and finances) were scarce.

                                              As you guessed, I have no experience scraping bearings or housings and I'm reluctant to try on such a project. Perhaps on another, more easily replaced part, I will try it.

                                              My intention is now to clean up the parts as much as possible (I'll use your petrol trick, thanks) and to reinstall them before adjusting as carefully as possible. I'll then measure the run out, try the lathe and see if I've made any improvements.

                                              Concerning the thrust bearing, I guess this should be reinstalled with a grease rather than relying on oil from the oiler cups. Will a general-purpose molybdenum grease be suitable?

                                              The second half of your message seems to have been lost – the first half has been posted twice, perhaps by mistake?

                                              Kind regards

                                              #468324
                                              Brian Wood
                                              Participant
                                                @brianwood45127

                                                Hello again Luke,

                                                Part 2 got lost so I will have to do it again from memory, most annoying.

                                                This stage describes the steps to rebuild the headstock

                                                Draw the bearing shells into the housings with a long bolt and wide flat washers either end to pull them in square. Don't draw the front bearing into the thrust bearing pocket. Make sure you have the oil holes on the correct side and that the split aligns with the gap in the housing

                                                Assemble the spindle and the thrust washer on their own into the bearings shells to see how the spindle feels in position when the bearings are slack. Oil the bearings and tighten first the rear, then the front and finally the thrust bearing [ Make sure there is a soft washer under the grub screw to avoid bruising the thread] Test the feel again, there should be detectable drag by hand on the spindle nose thread.

                                                If this feels OK pull the spindle out again and rebuild with the cone pulley and an intact bull wheel. You might have to increase the dimple depth for both grub screws, the one for bull wheel looked pretty well chewed up. Don't forget to fit the belt!

                                                Refit the 25 T gear. I think it had been fitted much too far on previously, just sufficient for full engagement with the reversing gears below it is correct. The gear will tap on with a soft faced mallet and test it is going on square. Also make sure the two halves of the 2 BA screw hole are aligned. Test with a screw for thread engagement without binding , then run a 2 BA tap in to refresh the thread. Cut somewhat deeper this time, blow out the swarf and fit a grub screw; Finish with thread lock

                                                Now set up the bearings again to just get drag on the spindle and run the lathe for 1/2 hour or so on a slack belt to bed things in. Feel the bearings as this test proceeds, they should not get warm. If all OK then tension the belt and run for a further hour, listening and feeling bearings during this time for signs of distress. Oil the bearings frequently as well.

                                                That will be sufficient I think for a usable machine. It will NOT be up to Dean Smith and Grace tool room standards of course, these machines sold fully equipped for £50 or so in their day

                                                A new thrust bearing if you need it can be bought from either of the following suppliers;

                                                Bearing Boys or Just Bearings. They both have websites

                                                I hope that helps and gives you some reassurance.

                                                Kind regards Brian.

                                                 

                                                 

                                                 

                                                Edited By Brian Wood on 01/05/2020 12:09:40

                                                #468366
                                                Howard Lewis
                                                Participant
                                                  @howardlewis46836

                                                  Looks to be in quite good condition. And fitted with tumbler reverse, (not all were )

                                                  So will be 3.5 centre height. The Mandrel thread started out at 7/8 BSW, (9 tpi )but changed to 7/8 x 12 tpi.

                                                  Possibly, so of the last ones produced may have even had what we now think of as Myford standard 1.125 x 12 tpi thread.

                                                  The Cross Slide Handwheel looks to be a shop made addition, possibly to overcome the odd increments of the original 80 division dial on a 12 tpi screw, giving a 0.00104" increment.

                                                  If you have a complete set of changewheels an additional 20T and 60T would allow you to set up for a fine feed of just over 0.004"/rev. For this, you may need to fettle the Mandrel end of the slot in the Banjo. The train is

                                                  20 : 60/20 : 65/20 ; 60 on the Leadscrew.

                                                  Brian will be far more able than I to state the trains for screwcutting various threads.

                                                  A quite useable machine. Possibly, someone came up with a modification to change the saddle traverse to that taken as normal, instead of the ex factory seemingly reverse action. (but it was made down to a price, when manufacturing was difficult, nearly 80 years ago )

                                                  Enjoy yourself with it!

                                                  HTH

                                                  Howard

                                                  Edited By Howard Lewis on 01/05/2020 16:02:16

                                                  #468374
                                                  Brian Wood
                                                  Participant
                                                    @brianwood45127

                                                    Hello Howard,

                                                    Thank you for the compliment, I hope I can live up to it.

                                                    Luke said at the start of this thread that the mandrel nose thread was 3.125 inch x 12 tpi, as well as giving the other parameters that were common to late issue ML4 lathes it is the same model that my Dad bought new in 1945 and I was allowed to use as a 7 year old.

                                                    That nose thread would be ripe to accept a simple collar modification to allow ML7 spindle fitting hardware to be used, I don't know what other chucks he has inherited.

                                                    Thus far we know nothing about the state of the Morse tapers. I am hopeful that they have survived unscathed after all these years. We also know very little about the state of the bed. It is very likely to be worn at the chuck end, but that of course doesn't mean the lathe cannot be used—it just needs due allowances for age

                                                    Like you, I thought this could be restored to a fair working machine, Luke seems to be capable and with the family history of ownership from Grandfather—Father—Son it seems only fitting to get it fully operational again.

                                                    Regards Brian.

                                                     

                                                    Edited By Brian Wood on 01/05/2020 16:50:27

                                                    #468383
                                                    Luke Mitchell
                                                    Participant
                                                      @lukemitchell30627

                                                      Hi both,

                                                      I've included an image showing the ways (I posted it originally but I no longer trust Google and so I've re-uploaded it, elsewhere). They are indeed a little worn near the chuck, and a little discoloured at the far end beyond where the tailstock usually sits, but they still appear to be flat and mostly true. There is a slightly tight spot in the middle of the bed that it can be a little difficult to get the tailstock past but it's nothing to complain about.

                                                      If I can get the rest of the lathe running reasonably true then I will investigate regrinding the ways and re-seating the saddle. If possible (and particularly due to the history of the lathe, as you say Brian), I would like to restore it working order in the best way possible. I'd need to contact a local machine shop and get some quotations for this work but I fear it will be rather expensive.

                                                      The tapers seem to be in good condition. The headstock is bored to MT2 whilst the tailstock accepts MT1 tooling. I haven't noticed any wear to either and the tooling I've used fits snugly – indeed it becomes quite difficult to eject from the tailstock and needs to be knocked out with a wooden dowel and a mallet. Many other lathes, I notice, are abke to auto-eject tooling. Perhaps that was a later development.

                                                      I've used the tailstock taper quite a bit to support work (a necessity given the play in the headstock and, I suspect, a slightly worn 3-jaw). I've also used it for drilling and reaming and it performs well at both tasks.

                                                      It did take me some time to get the tailstock properly aligned to the headstock and the first few holes I drilled we a little off-center. Once I'd managed to slackened off the bolt holding the castings together I could use the set-over adjustment, a knurled wheel on the rear, to center the points of a taper held in both tailstock and headstock. The tailstock is still a touch lower than the headstock and I will have to use some shim stock to raise the casting. I'd also like to purchase a test bar to make sure my adjustments are accurate. (But all of this after the headstock bearings are in order).

                                                      Workholding-wise: I have a 3-jaw self-centering chuck ("British Crown", fitted in the photographs), a 4-jaw independent chuck ("British Crown&quot and a spare 3-jaw that I need to restore. As I mentioned, the 3-jaw doesn't hold stock very true and I suspect the jaws are worn unevenly. Any information about this would be appreciated but, if I can get everything else tightened up, I will look into grinding them concentric in-situ using a toolpost grinder (which I'll have to buy/make/cobble).

                                                      I have the original toolpost, which is a simple vee-shaped piece of steel with some patterning for grip, but I believe it's missing a spring and a secondary bolt. It's on my list to make up these missing pieces so the original toolpost can be used again.

                                                      I've installed an Indian-made Dickson-style QCTP as I quite quickly got fed up of shimming up tools to the center height. It's not the best quality but it works well, especially after I made up a brass bushing to grip the supporting bolt a little tighter. On this note, as I think I mentioned, somebody has previously re-threaded the tool post bolt on the top-slide for M10. I don't know if the original thread had worn or whether there was another reason.

                                                      Posted by Brian Wood on 01/05/2020 16:49:52:

                                                      That nose thread would be ripe to accept a simple collar modification to allow ML7 spindle fitting hardware to be used, I don't know what other chucks he has inherited.

                                                      Brian, when you say this, do you mean the spindle wont accept ML7 hardware as it is? I was under the impression that, given the thread form and dimensions, ML7 backplates etc. would fit. May I ask what the difference is?

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